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custom turbo kit!!! Dyno Sheet up update on pg.10

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Old 03-20-2010, 09:42 PM
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Default Re: custom turbo kit!!! Dyno Sheet up update on pg.10

Originally Posted by ElevationTC



woow.. sorry to hear this man!
Still got that block mike lol
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Old 03-20-2010, 09:48 PM
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dude thats like what happened to me kinda... except my cylinder 1 was the 0... but there was fuel.... we have no idea what failed on my motor but it coulda been a number of things except my plug was crushed.. mike you think these 2 could be related? Could it be failed stock sleeves? No fuel return setup the cause? Meth? hmm im sorry to hear this marcelo :/ back to stock motor like me? i know it sucks bro
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Old 03-20-2010, 10:02 PM
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Default Re: custom turbo kit!!! Dyno Sheet up update on pg.10

Originally Posted by SoFloTC
dude thats like what happened to me kinda... except my cylinder 1 was the 0... but there was fuel.... we have no idea what failed on my motor but it coulda been a number of things except my plug was crushed.. mike you think these 2 could be related? Could it be failed stock sleeves? No fuel return setup the cause? Meth? hmm im sorry to hear this marcelo :/ back to stock motor like me? i know it sucks bro
Nah playa I'm not going back to stock just hopefully I can fix that cylinder. If I have to go back to stock this car is going to carmax.
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Old 03-20-2010, 10:03 PM
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Originally Posted by SoFloTC
dude thats like what happened to me kinda... except my cylinder 1 was the 0... but there was fuel.... we have no idea what failed on my motor but it coulda been a number of things except my plug was crushed.. mike you think these 2 could be related? Could it be failed stock sleeves? No fuel return setup the cause? Meth? hmm im sorry to hear this marcelo :/ back to stock motor like me? i know it sucks bro
i dunno ur plug was messed up before i messed with the car... Maybe luggis timing or something else?
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Old 03-20-2010, 10:10 PM
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Originally Posted by m6ar2cel6oTC
Nah playa I'm not going back to stock just hopefully I can fix that cylinder. If I have to go back to stock this car is going to carmax.

lol carmaxxxxx! hmm thatll be tough i hope you can get it done gotta tear the motor apart and see what failed hmm GL!
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Old 03-20-2010, 10:31 PM
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marcelo no worries bro... some hialeah sauce will cue all that ____ right up! you'll be back on top in no time!
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Old 03-20-2010, 10:35 PM
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Default Re: custom turbo kit!!! Dyno Sheet up update on pg.10

Originally Posted by TCpete
marcelo no worries bro... some hialeah sauce will cue all that ____ right up! you'll be back on top in no time!
Yeah on top of another car. I'll buy a used engine thorw it in sell everything else and call it a day.
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Old 03-21-2010, 01:20 AM
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if you part out i have dibs on your manifold and downpipe. muahahaha. sucks to hear this marcelo....really does. it doesnt sound like the stock sleeves failed, sounds more like timing. luiggi didnt even use a knock detector did he?

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Old 03-21-2010, 01:45 AM
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Default Re: custom turbo kit!!! Dyno Sheet up update on pg.10

Originally Posted by gingles
if you part out i have dibs on your manifold and downpipe. muahahaha. sucks to hear this marcelo....really does. it doesnt sound like the stock sleeves failed, sounds more like timing. luiggi didnt even use a knock detector did he?
Nah. But after the tune I did get 3" exhaust, went full meth and got bigger intercoolr piping. So I guess that made a big enough difference on the tune. Bro like I was telling rob my car felt the strongest it has ever felt after I put that 3 " and full meth. I felt like I had a hell of alot more then 429whp and 409trq. The look on the guys face of the guy on the bike was priceless.
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Old 03-21-2010, 01:58 AM
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Originally Posted by m6ar2cel6oTC
Nah. But after the tune I did get 3" exhaust, went full meth and got bigger intercoolr piping. So I guess that made a big enough difference on the tune. Bro like I was telling rob my car felt the strongest it has ever felt after I put that 3 " and full meth. I felt like I had a hell of alot more then 429whp and 409trq. The look on the guys face of the guy on the bike was priceless.


What kind of bike?

my 600 did 10.4@125

Slip on, K&N filter. and tuned

So you were ____ing hauling ___
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Old 03-21-2010, 02:21 AM
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Default Re: custom turbo kit!!! Dyno Sheet up update on pg.10

I have no clue what kind of bike. I'm not a bike person all I know is it was silver and pretty nice. It was a crotch rocket. Lol
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Old 03-21-2010, 02:22 AM
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Default Re: custom turbo kit!!! Dyno Sheet up update on pg.10

Memories. Lol
Attached Thumbnails custom turbo kit!!! Dyno Sheet up update on pg.10-imageuploadedbytapatalk.jpg  
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Old 03-21-2010, 11:52 AM
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Originally Posted by m6ar2cel6oTC
Nah. But after the tune I did get 3" exhaust, went full meth and got bigger intercoolr piping. So I guess that made a big enough difference on the tune. Bro like I was telling rob my car felt the strongest it has ever felt after I put that 3 " and full meth. I felt like I had a hell of alot more then 429whp and 409trq. The look on the guys face of the guy on the bike was priceless.

You didn't tune the car after adding a 3" and Meth injection? Brah...shouldn't do things the hard way, turns around and bites you.
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Old 03-21-2010, 03:07 PM
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i was already tuned on 50/50 meth and distilled water but since it kept messing up my TB i decided to just go 100%meth. the funny thing about it was i was gonna have it retuned by luiggi but then again i saw my afr good s i said i'll wait. but then again me and rob were thinking my wideband was off. i guess it was or the timing was way off after adding some goodies. now i just dont know when it will get torn apart to see the damage.
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Old 03-21-2010, 03:20 PM
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Switching to 100%meth would offer better fueling to the car, but accually cause less intake charge cooling possible creating knock... Should of left it at 50/50 or 60/40 which is been proven to offer best cooling charge.

People who use 100% meth are using it more as a fuel..
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Old 03-21-2010, 03:26 PM
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^^ Exactly!

Poor marcelo i'm trying to convince him to open up the motor to see what the actual damage is, then hopefully he can just fix what is needed and stay boosted with a built motor.
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Old 03-21-2010, 03:28 PM
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Originally Posted by B_Real45
^^ Exactly!

Poor marcelo i'm trying to convince him to open up the motor to see what the actual damage is, then hopefully he can just fix what is needed and stay boosted with a built motor.


By the looks of his plug he probably broke a ringland or burned a hole right in the piston. Im assuming you drove it or let it run after this happened..

If not then the issue was happening over time!.

I mean it sucks dude no matter what! But what made u go 100% meth?
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Old 03-21-2010, 03:51 PM
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Originally Posted by ElevationTC
By the looks of his plug he probably broke a ringland or burned a hole right in the piston. Im assuming you drove it or let it run after this happened..

If not then the issue was happening over time!.

I mean it sucks dude no matter what! But what made u go 100% meth?
changing 6 TB's! lol it had to be the water causing it to corrode in the TB and get the sensor gear stuck not letting it open. so figured to do 100 meth! since it dissolves alot faster then the water. i guess i'll try 60/40 % again or 70/30% i'm just damn tired of switching out TB's. either way i dunno whats gonna happen to this car. way to much money put in and not enough results. lol
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Old 03-21-2010, 04:23 PM
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Marcelo - not enough results?

You have made 427whp on the following:

"eBay" parts - piping, intercooler, manifold.

60-1 $600 turbo

700cc injectors with no fuel return

50% meth

ON A PIGGYBACK.

Those are good results. I think you just should have tuned again after the exhaust - and should always change your w/b sensor now and then.
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Old 03-21-2010, 04:27 PM
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Default Re: custom turbo kit!!! Dyno Sheet up update on pg.10

W/b sensor? Lol. Yea good results but for how long lol. Only thing that sucks is I paid off 4 of my credits cards and still owe a couple thousand on the wedding stuff and trying to buy a house and now I have to rack up my cards again cause of my car.
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