Dezod Turbo Kit ****PICS****
#43
i dunno the cause of the first blown engine but the only thing i can think of is, about 4 months prior i had some water damage with a cold air intake, and got it hydra-locked, but i fixed it and it ran fine....like brand new....then i put the turbo kit on it was great then i started to have multiple random misfires, couldn't figure it out it wasn't the plugs, nor wires, nor coils or anything to that nature bc i got them tested and then all of the sudden i went to go get something to eat came out of an intersection not even into boost and then the bytch just blew shy high....not as bad at this time though....the place that tuned it, is PRO MOTION TUNING out of fredericksburg, VA AKA (CreativeCompacts.com) for real STAY AWAY they don't know what the hell they are doing.
#46
Originally Posted by TURBO_TC02
i dunno the cause of the first blown engine but the only thing i can think of is, about 4 months prior i had some water damage with a cold air intake, and got it hydra-locked, but i fixed it and it ran fine....like brand new....then i put the turbo kit on it was great then i started to have multiple random misfires, couldn't figure it out it wasn't the plugs, nor wires, nor coils or anything to that nature bc i got them tested and then all of the sudden i went to go get something to eat came out of an intersection not even into boost and then the bytch just blew shy high....not as bad at this time though....the place that tuned it, is PRO MOTION TUNING out of fredericksburg, VA AKA (CreativeCompacts.com) for real STAY AWAY they don't know what the hell they are doing.
maybe you got a bad kit or something. don't excuse the kit itself, comb over it with a fine tooth to make sure next time (if there is going to be a next time), that your kits components are properly installed, so that when you build the motor all that work doesn't go to waist and you mess THAT engine up too.
#47
Originally Posted by rhythmnsmoke
Originally Posted by 318_tC
Holy snap son!
Running rich did this? Hmmm...I run 10.0 all day every day beating the poop out of the car...
Running rich did this? Hmmm...I run 10.0 all day every day beating the poop out of the car...
I don't recall seeing a motor blow from being rich.... Very puzzling.
#48
Originally Posted by kytc
Originally Posted by rhythmnsmoke
Originally Posted by 318_tC
Holy snap son!
Running rich did this? Hmmm...I run 10.0 all day every day beating the poop out of the car...
Running rich did this? Hmmm...I run 10.0 all day every day beating the poop out of the car...
I don't recall seeing a motor blow from being rich.... Very puzzling.
I'm sure that is true. But giving the history of the F/I on a "Scion tC", we have yet to see any blown motors due to rich A/F conditions. A large % of the turbo guys are/have been riding on A/F readings in the 10's and 11's, and have been doing for quite some time now.
#50
Misfiring issue!!!
Originally Posted by 318_tC
random misfires huh? was you throwing CEL's?? Ive got a misfire in cylinder 2 now that im trying to figure out
#51
Originally Posted by TURBO_TC02
damn tunind shop that tuned it screwed it up and was running rich in cylinder one...waayyyyy rich and the fuel pooled in the cylinder and it wasn't combusting correctly and it was misfiring, so when i fixed the miss-fire, i drove it home and got about a block from the house and when i punched it, it completely blew sky high...the whole stree i was on turned into a smoke screen ally-way. I was only running 5 PSI too pretty sorry shyt to be happening at 5 PSI huh?
#53
no i had just got it tuned the weekend prior and i blew it on a tues...and it was running like a beast....and then all of the sudden one after, i started to get the misfires, its wierd though bc when i tried to figure it out i found out that i had a vaccum leak coming from the boost controller and so i took it off and then connected the vaccum line str8t up to the wastegate w/o the the controller, and then i had no problems but then again from the enging running rich, all of the fuel that was being transmitted was pooling in the cylinder and then when it was running correctly thats when it decided to blow
#54
no i had just got it tuned the weekend prior and i blew it on a tues...and it was running like a beast....and then all of the sudden one after, i started to get the misfires, its wierd though bc when i tried to figure it out i found out that i had a vaccum leak coming from the boost controller and so i took it off and then connected the vaccum line str8t up to the wastegate w/o the the controller, and then i had no problems but then again from the engine running rich, all of the fuel that was being transmitted was pooling in the cylinder and then when it was running correctly thats when it decided to blow
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my06tc
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06-25-2015 12:18 AM